The morning came and I was out there first thing putting on the fuel pump relays and the power relays. After doing a bit of troubleshooting with the fuel pump relay it managed to start. It was an extremely tense moment as wrong connections could have ruined everything. It started and idled nicely.
Ben Jay came along and started helping me out by doing a oil, filter and spark plug change. Niall then shortly turned up with the magic parts! A gti6 PAS pump and some GTI6 injectors. Thought these were a good idea as they provide a lot more flow than the 1.8 ones.
Niall left and Ben and I fitted the new PAS pump. Unfortunately the belt I had bought months ago specifically for the job was too short so Ben had to do several runs to ECP in order to get the right one... Which turned out to be not 1103 but 1145. I still dont know what caused it to be so wrong.
With time pressing and there being a severe lack of vices on the street I couldnt rotate the elbow on the PAS pump so I decided not to plumb the PAS.
There were a few things that didnt have connections any more... There was no vacuum take off for the assisted breaking and the top breather hose had no where to go so that was stuffed into a coke bottle. Remember bodged not bought people!
Then the trumpets and filter housing went on. Followed by the filter itself!
Luckily I remembered I had a spare breather filter! (See if you can spot the mistake in the picture above and below! D: )
With an hour to go before the flat bed was due to arrive we changed the fuel filter and put the car back on the floor. Ben headed home and I sat and waited.
Allen the very optimistic flat bed man arrived and put out the ramps and lots of wooden chocks which meant I got onto the ramp fine. The last big of getting onto the truck was a bit more of a struggle as the car was scraping the entire way! Being low isnt cool kids, its just embarassing!
Amazingly for the first time in my pug ownership the car was on the back of a truck. Not for breaking down. Just for starting another stage of its life.
The car refused to come off the truck and got its exhaust stuck on the lip of the truck. Some more wood sorted this out.
Lack of photos here but Niall turned up again and we waited for an hour and a half for a 1.8 MG ZR to come off the rollers. That made 202hp and the old man said it was his wifes. He was lovely and very chatty and it was great to see someone so passionate about cars at such an old age.
With the GTI6 injectors the car didnt idle so we had to push it onto the rollers. Steve the super hero mapper found that my bodies were missing a spring which meant the butterfly valves were in the wrong position. Nothing I lost and thats what you get for second hand parts. 5 minutes in a back room saw him find one which fixed it.
They also needed to put their lambda sensor in. Apparently mine was made of rust and they had to use a blow torch on it. That made relations better no end.
Car went on the rolling road and lots of air conditioned air was flowing through the radiator. Very useful as like most things original on this car... they didnt work!
They made sure to tie it down properly as they hadnt seen this much french power before! I asked for the limiter to be at 7000rpm.
Steve went about doing his job whilst the extractor did a very poor job of sucking up all the fumes.
After about 4 hours we had ourselves a laminated print out!
129.4hp and 121lbft of torque. Not bad for an engine (125k) which is 110hp stock.
Took it for a quick test on the road which was interesting with no PAS or assited brakes. It sounds amazing and it shifted a whole lot more than it used to. Handed over what remained of my overdraft and convoyed home with Ben!
This is how it stands today. Working with only the loom to tidy up and the PAS and brakes to fix.