17-06-2014, 08:37 PM
Bit of an update is required on this really. Was away for FCS the other weekend so didn't get chance to do anything but made a start to get cracking with it on the Monday. Got the new matrix fitted back in after a bit of swearing which seemed to help. Heat box all bolted back in, then dash etc. So all bolted back in and of course a few issues. Brake light was staying on which was cuz i forgot to check the brake light switch was in when the dash went back in so sorted that and also the heater fan didn't work which turn out to be the motor not working from lack of use. When Mike and james popped over mike took the motor out and freed it up. Any way didn't get and pics of the dash going back in but it was pretty much all back together and Mike and James popped over last friday to try and get it all finished.
James had some hdi 266 brakes to fit as he had new discs and pads so we got them on with 1 slight issue as i was cleaning the hub threads for the carrier bolts with a thread chaser i managed to snap it off so had to get that out some how. Tried a few ways to get it out including some heat
In the end Mike welded a nut on and we got it out and got the brakes fitted. Jimbo checking the brakes are fitted correctly
And mike was taking some pics of my legs while i was sorting the brakes
As the car had been sat of over a year it had some surface rust underneath and in the arches which Jimbo cleaned off and sprayed with some under seal to try and look after it
I got James to wined the coil overs up a bit as couldn't get it on the mot ramp. Then went to drive it onto the mot ramp, james drove it up and down out side the workshop to bed the brakes in a bit and another issue, we had a bang and both wheels pointing into the middle. The inner rack joint had come out for some reason. So with a bit of effort got it back on the ramp to see what had gone on and seemed like someone had fitted an inner rack joint but used a washer they shouldn't of and damaged the threads on the joint bit. We couldn't really do much more so left it for the night.
Mike popped over again Saturday armed with another steering rack but threads looked fine in the steering rack so popped another inner rack joint on and made sure it was tight and screwed in ok. So Mike got that all sorted
Also Mark popped over armed with his 'milkers' as usual and lent a hand and popped a tyre on
Got everything sort and got it MOTed. That morning i had popped to Southampton to pick up some ph1 gti6 half leathers and Jmaes was after some so sorted him out with some and fitted them. Gave it a clean while the seats were out.
Thats about it. We got it over to James's last night and im sure he will update with the plans/progress from now on
James had some hdi 266 brakes to fit as he had new discs and pads so we got them on with 1 slight issue as i was cleaning the hub threads for the carrier bolts with a thread chaser i managed to snap it off so had to get that out some how. Tried a few ways to get it out including some heat
In the end Mike welded a nut on and we got it out and got the brakes fitted. Jimbo checking the brakes are fitted correctly
And mike was taking some pics of my legs while i was sorting the brakes
As the car had been sat of over a year it had some surface rust underneath and in the arches which Jimbo cleaned off and sprayed with some under seal to try and look after it
I got James to wined the coil overs up a bit as couldn't get it on the mot ramp. Then went to drive it onto the mot ramp, james drove it up and down out side the workshop to bed the brakes in a bit and another issue, we had a bang and both wheels pointing into the middle. The inner rack joint had come out for some reason. So with a bit of effort got it back on the ramp to see what had gone on and seemed like someone had fitted an inner rack joint but used a washer they shouldn't of and damaged the threads on the joint bit. We couldn't really do much more so left it for the night.
Mike popped over again Saturday armed with another steering rack but threads looked fine in the steering rack so popped another inner rack joint on and made sure it was tight and screwed in ok. So Mike got that all sorted
Also Mark popped over armed with his 'milkers' as usual and lent a hand and popped a tyre on
Got everything sort and got it MOTed. That morning i had popped to Southampton to pick up some ph1 gti6 half leathers and Jmaes was after some so sorted him out with some and fitted them. Gave it a clean while the seats were out.
Thats about it. We got it over to James's last night and im sure he will update with the plans/progress from now on