21-11-2012, 08:34 PM
Before I go ripping the car to pieces tomorrow, can anyone suggest any reason for this happening?
Compressor housing popped loose as I came back from a test run. It appears the securing washers have bent and allowed it 2-3mm away from the seal.
My thoughts are that.. where I moved the actuator, I used my own bolts and washers to clamp the turbo after clocking it. Is it likely that the washers I used were the wrong size/too weak, and boost pressure overcame them?
Or is something more sinister at work considering oil is leaking out?
Suggestions please...
Compressor housing popped loose as I came back from a test run. It appears the securing washers have bent and allowed it 2-3mm away from the seal.
My thoughts are that.. where I moved the actuator, I used my own bolts and washers to clamp the turbo after clocking it. Is it likely that the washers I used were the wrong size/too weak, and boost pressure overcame them?
Or is something more sinister at work considering oil is leaking out?
Suggestions please...